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D7629/25279 - Initial Restoration

The loco wasn't considered serviceable at purchase. Known faults were the liner topseal and seized turbo. The loco also was fitted with commercial HGV batteries which were patently not up to the load and rating required for traction.

The batteries were therefore never used again, being replaced with a new set of traction batteries of the correct design for this type of locomotive from Deta. The Turbo was scheduled for overhaul, and the cylinder head prepared for removal to address the topseal. However, further inspection revealed serious wear on the exhauster and auxiliary generator brushgear, and a set of main generator brushgear (which had caused flashover damage). The bodywork was suffering from corrosion to the point of holes, but the initial work was to be concentrated on the electrical and mechanical systems. The restoration of the loco to working order would be a significant task.  The full story is relayed in the Restoration Diary.

D7629 AVR Detail

The cylinder head has been removed, showing water damage

Cylinder heads removed exposing damage

The loco has two cracks (just visible), which date back into BR ownership.

It can be seen that the cracks were drilled to stop them - which has been successful. The cracks have not grown since this work was done in BR days. The bogie design suffered from specific weaknesses causing these cracks.

Shot showing electrical cubicle details.

25265 and D7629 pose at Rothley, GCR

Contractor John Robinson working to address the bodywork corrosion

New bodywork platework.

New bodywork platework.

There were corrosion holes in these locations.

Note the aperture cut for new bodyside steps, which John Robinson fabricated.

The failed turbo is removed from the loco

A view of the turbo during dismantling (turbine end).

Initially the turbo was subject to work at Rothley. This shows the unit partially dismantled.

A view of the turbo shaft. The bearing is severely worn and the shaft (turbine end to right), shows severe heat damage

Detail of severe damage to the turbo shaft (turbine end)

Rebuilt turbo (Impeller end)

Rebuilt turbo (turbine end).

After a further failure, the turbo was sent to Marine Turbo Engineering at Birkenhead for a full overhaul. This view shows the unit after replacement

The shaft was found to be 26 grammes out of balance - a significant degree.

The team present after refitting the overhauled turbo to the loco.

Darren Fawcett, Dave Partner and Martin Clark. (Mark Fowler out of shot).

The main and auxiliary generator after cleaning.

No5 piston is removed.

No5 piston emerges from the block

No5 piston removal

No5 piston craned clear of the block

No5 piston emerging from the loco

No6 fuel pump replaced with overhauled unit.

The buffers had become weak and were replaced.

The cleaned and treated block.

Cleaned and painted block.

No5 liner showing the failed topring.

No5 liner topseal removed.

No5 pot

No5 liner removed.

The head is replaced and shows transition seals (new).

No5 topseal ring - corroded to total failure.

Dave Partner and Darren Fawcett - both of whom gave significant help to get D7629 back into traffic.

D7629 and D1705 on D7629's first test run at Rothley, GCR.

Mark Fowler, next to D7629 on the occasion of the loco's first test-run.

After it's move to Ruddington (GCRN), the opportunity was taken to bestow the loco with full yellow ends for a Diesel Gala.

The loco moved to GCRN (Ruddington) after two successful seasons at GCR

Full yellow ends being applied to D7629 at Ruddington

 

 

 

This page last updated: 22 February 2006